Room
for a View
Signs
of Stress at Indian Point
by Todd Paul
On February 27,
2001, the Deputy Director of the Nuclear Regulatory Commission’s Division
of Reactor Safety sent a letter to the Senior Vice President of Consolidated
Edison’s Nuclear Operations division, Indian Point 2 Station. The letter
concerned a former employee of the Wackenhut Security company, who had
been fired after complaining about having to work excessive overtime
at the Indian Point 2 nuclear plant in Buchanan (Westchester County).
Since an OSHA investigation had concluded that discrimination was a
factor in the guard’s termination, the NRC wanted to know what Con Ed
was doing “to assure that this matter is not having a chilling effect
on the willingness of other employees to raise safety and compliance
concerns within your organization and... to the NRC.” As of press time,
Con Ed had not responded to the query. Protection of nuclear plant whistleblowers
is crucial, especially because, according to critics, the NRC relies
on them to bolster inadequate inspections and lax regulation of the
nation’s aging nuclear reactors.
(On March 4, 1996, Time’s cover story on the Millstone reactor trumpeted,
“two gutsy engineers in Connecticut have caught the Nuclear Regulatory
Commission at a dangerous game it has played for years: routinely waiving
safety rules to let plants keep costs down and stay on line.”)
According to a
1999 Public Citizen report titled “Amnesty Irrational,” three nuclear
reactors—Haddam Neck in Connecticut, Maine Yankee and Millstone Unit
1—have been shut down by the NRC due to “design basis” issues—that is,
the reactors were being operated illegally outside the safety parameters
established in their operating licenses. In every case, according to
Public Citizen, it was whistleblowers and public protest, not NRC diligence
and enforcement, that caused the plants to be shut down. An overworked
security guard may not be cause for general alarm. But the case points
up a recurring problem at Indian Point 2. In March, the New York Times
reported that an engineer working for a contractor at IP2 quit “in a
dispute over the reliability of the system that triggers automatic shutdowns
during equipment failures.” The engineer had discovered that the reactor’s
safety systems had been modified in ways that were not reflected on
the plant’s blueprints. That means anyone attempting to fix these systems
during an emergency would encounter wiring different from the plant’s
specifications. The problem is equivalent to rewiring the circuits in
your house, neglecting to write down the new system, and then trying
to figure out which fuse to replace when the lights go out. This problem
was cited in a recent NRC inspection of IP2, along with substandard
programs for finding and correcting problems, equipment reliability
issues, procedural weaknesses and shortcomings in engineering support.
A third employee
of IP2 also resigned recently due to frustration with the plant’s safety
systems. According to the August, 2000 Albany Report, published by Environmental
Advocates, a proposed New York State Whistleblower Protection Act passed
the Assembly but was never voted on in the Senate. Sponsored by Assemblyman
Richard Brodsky and Senator Thomas Morahan, the WPA would have established
a state nuclear power plant whistleblower access and assistance program.
The bill was defeated thanks in part to opposition from industry lobbyists
like the Energy Association of New York State, of which Consolidated
Edison is a member. Joe’s Story “Joe” (not his real name) is an employee
of Con Edison. For five years he served as an A-grade mechanic on a
power generation maintenance crew at IP2. When there was an outage,
Joe and his crew were called in to get the reactor fixed, and fixed
fast. He recalls working 118-hour weeks for four straight months during
one outage at IP2. That’s nearly 17 working hours per day, seven days
per week. Joe was lucky—he lived near the plant. Others on his crew
had to spend two of their seven free hours commuting to and from homes
in Brooklyn, if they went home at all.
That means some
of the people responsible for repairing an aging, accident-prone nuclear
plant, which sits 24 miles from New York City astride the Ramapo fault
line, were getting, at most, five hours of sleep per night for four
months—assuming they didn’t eat, bathe, or spend time with their families.
This kind of scenario is business as usual at Indian Point, according
to critics of Con Ed, who say the utility company values dollars over
safety. The New York State Power Authority, which operates the neighboring
Indian Point 3 reactor, doesn’t do much better. While people like Joe
were scrambling to get IP2 back on-line after the radioactive steam
release of February, 2000, dozens of workers were contaminated during
what should have been a routine refueling of IP3. The cause? In order
to cut costs and off-line time, NYPA knowingly and illegally relaxed
the protective clothing requirements for workers over a 40-day period.
The cooling fans in the reactor dome were broken, and NYPA claimed that
heat exhaustion was a bigger threat to worker safety than exposure to
radiation. Joe knows all about the hazards of working in a nuke plant.
He and his crew used to lie in puddles of radioactive water, fixing
a turbine or steam tube, “till you got burned up a little bit.” One
time the boss told Joe’s crew to don extra jumpsuits, earmuffs and towels
around their necks, and climb on top of the generator turbine to loosen
every other bolt. The extra garb was to protect them from the pressurized
steam, which would shoot out of the turbine at 150 degrees as soon as
a bolt was loosened. Nevertheless, Joe says, “My lifetime exposure [to
radiation] was low—it was five rems. Other guys were up to 48 rems.”
The NRC’s annual maximum whole body (internal and external) exposure
limit is five rems; its annual skin exposure limit is 50 rems. According
to the Pacifica Radio Network, IP2 was cited in the early 90s as the
plant that was producing the highest level of radiation for workers,
with the least control on worker safety.
Does Indian Point
2 pose a danger to the public? Joe says no, despite his belief that
accidents are both more numerous and more serious than the public has
been led to believe. For example, Joe cites a reported leak of five
gallons of radioactive water. In the locker room at the plant, the guys
who were called in to fix the leak told Joe the true figure was more
like 150 gallons. Frequently, he says, Con Ed sacrifices safety and
misleads outsiders in order to enhance the plant’s public image—which,
considering the dismal public image of IP2, speaks poorly of true conditions
at the plant. However, Joe believes there are enough backup systems
in place to prevent a disaster at IP2, even though, “more often than
not, they’re relying on the backup systems.” It’s a good thing there
are numerous backup systems, because given the millions of people living
within 50 miles of Indian Point, many believe any emergency evacuation
plan to be an exercise in futility. “If there’s an explosion and an
immediate release of radiation,” Joe admits, “the people are fucked.”
Joe no longer works at IP2. Concerned about his health, he transferred
to another division of Con Edison.
He asked that we
preserve his anonymity in order to protect his job. A History Of Failure
Many anti-nuke activists consider Indian Point to be a disaster from
inception, considering that Unit 1 was built on an earthquake fault
line 24 miles from the most populous city in America. At the time, the
Atomic Energy Commission had no siting criteria for reactors. Unit 1,
also operated by Con Ed, had no emergency core cooling system and was
forced to close in 1974; but because the site had already been approved
for a reactor, units 2 and 3 were allowed to be built there, despite
the fact that the site failed five of six criteria under 1979 NRC siting
rules. Consider this partial chronology of incidents at Indian Point
between 1979 and 1994, compiled by Citizen’s Awareness Network (a complete
list is available online at http://www.nukebusters.org/html/indian_point.html):
Sept 1979: The Union of Concerned Scientists, NYPIRG, and WESPAC petition
the NRC to decommission (dismantle) the inoperative IP1 and suspend
operations at IP2 and 3, citing over 60 safety deficiencies, including
problems in plant design. Oct 17, 1980 to 1982: Con Ed discovers over
100,000 gallons of radioactive water spilled in the containment building
of IP2. No one had checked the area since Oct 3, despite warning lights
showing water build-up. Con Ed attempts to restart the reactor three
times, without first checking on possible damage from the spill. A UCS
study shows 24 equipment failures and 21 management and operations errors
in the period from Oct 1 to 20. IP2 is shut for eight months; Con Ed
attempts to recoup losses from the shutdown, estimated at $800,000/day,
with a 10 percent rate hike. 1980-82: NRC hearings on IP operations
and emergency planning are stalled when the hearing board chair resigns
in protest of a ruling that excludes much anti-nuclear testimony.
Former NRC Commissioner
Peter Bradford states afterwards, “Nowhere has the commission majority’s
hostility to fundamental legal concepts of fairness been more clearly
shown than in the Indian Point hearings.” Dec, 1992: The FBI seizes
NYPA records regarding a meeting at which a senior plant manager knowingly
lied to the NRC; in addition, the FBI seizes records showing that 25-30
plant operators admitted to “occasionally” falsifying log entries. June-Oct,
1993: NRC fines NYPA $300,000 for 17 safety violations, including defects
that caused a six month failure in a backup reactor shutdown system.
NYPA also admits that it has been issuing inaccurate reports on radiation
releases for 13 years. The NRC’s resident inspector notes, “They released
more (radiation) than they thought they released.” Nov, 1993: Two original
safety valves at IP3 found to be insufficiently rated; in the rush to
replace them before an upcoming NRC inspection, engineers install them
backwards, blocking both cooling systems and disabling backup generators.
May, 1994: After an NRC directive forces the utility to inspect its
spent fuel pool at IP1, Con Ed admits that water has been leaking for
four years, with estimates of up to 150 gallons of radioactive water
leaking each day. In a year-old rating procedure intended to be more
easily understood by the public, the NRC rates crucial safety systems
of nuke plants with a simplistic “green/yellow/red” designation.
Currently, Indian
Point 2 has the dubious distinction of being the only reactor in the
country ever to earn a red safety rating from the NRC. In an August,
2000 letter to Con Ed, the NRC concluded, “Despite opportunities [to
take] appropriate corrective actions... [steam] tubes with primary water
stress corrosion cracking... were left in service following the 1997
inspection [by Con Edison], until the failure of one of these tubes
occurred on February 15, 2000, while the reactor was at 100 percent
power.” The resulting radioactive steam release earned IP2 the nation’s
only “red” rating for barrier integrity. Chris Olert, spokesman for
Con Edison, says his company disagrees with the “red” rating. (Con Ed
contested the rating, but the NRC recently reaffirmed it.) Olert also
says the company is of “different professional opinions” with the engineer
who resigned, and asserts the company position that it’s not unusual
for on-paper technical specifications to occasionally differ from reality.
He believes the plant’s emergency plans are adequate and states, “The
plant’s operating safely.” Reactor Safety and the UCS Despite their
history and current poor safety ratings, the two operating reactors
at Indian Point are inspected only half as often as required by federal
law, according to the Union of Concerned Scientists, a 31-year-old nonprofit
formed to look at issues of science and technology. Dave Lochbaum is
the current UCS Nuclear Safety Engineer. His predecessor at UCS was
Bob Pollard, coincidentally a former NRC project manager for Indian
Point 2. Pollard resigned from that post during a “60 Minutes” interview
in 1976, saying he couldn’t continue to sign documents saying the plant
was safe. He called IP2 “an accident waiting to happen.” According to
Lochbaum, the steam tube rupture at IP2 in February 2000 was imminently
preventable. In fact, IP2 was the only plant in the country at that
time still using the old, outdated Westinghouse Model 44 steam generators.
Ten percent of the steam tubes in these generators had already been
plugged due to previous problems. Furthermore, Con Ed had already purchased
new generators, which sat unused at IP2 for a decade prior to the accident,
waiting to be installed. According to a petition sent from UCS to the
NRC following the February 2000 accident, “Dr. Joram Hopenfeld of the
NRC staff first documented concerns with steam generator tube integrity
on December 23, 1991. More than eight years later, his concerns remain
unresolved.” The petition demanded that IP2 be shut down until all four
steam generators were replaced; until Dr. Hopenfeld’s concerns were
resolved; and until potassium iodide tablets were distributed to neighbors
of IP2 (these offer some protection in case of a large-scale radiation
release).
Furthermore, the
petition requested a public informational meeting be held in the vicinity
of IP2. The petition was denied by the NRC in December 2000, on the
basis that the generators had by that time been replaced voluntarily
by Con Ed, and no further action was necessary. The UCS is not some
anti-nuke activist group. Lochbaum says the UCS doesn’t want to get
rid of nuclear power—they just want the plants fixed. Lochbaum doesn’t
feel the public was harmed by the steam release of 2000. He notes, “More
radiation would have been released routinely over the next month.” Now
that the generators have been replaced, the UCS is primarily concerned
with emergency planning at Indian Point. According to Lochbaum, federal
guidelines say emergency plan testing has to be done every two years
at all US nuclear plants. But the NRC makes an exception for New York
State, Lochbaum says, because there are two sites in the state where
two reactors are under different ownership. Because of what Lochbaum
considers an illegal exception, NYPA and Con Ed each get away with testing
their emergency plans every four years, on an alternating schedule.
Back On-Line IP2 went back to full power in January, following the installation
of the four new steam generators, which was completed in December.
“The safe and methodical
full return to power of Indian Point 2 is a tribute to our hard working,
dedicated employees,” said Kevin Burke, president of Con Edison. The
quick return of the plant to full operating capacity was important to
Con Ed for several reasons. For one thing, an idle nuke is a money-losing
proposition, while IP2 generates up to 1,080 megawatts and $1.4 million
in profits daily when fully operational. For another thing, Con Ed will
sell the plant to the Entergy company this summer, when the NRC is expected
to approve the license transfer. Entergy plans to purchase IP2 from
Con Edison for $602 million. Entergy purchased IP3 from NYPA in November
and is awaiting NRC license approval for that deal as well. A
third force acting on Con Ed at the moment is heightened scrutiny from
the NRC, anti-nuclear activists and local governments. The NRC just
completed an investigation of IP2, a full report of which was to be
made public shortly after press time (NRC reports, press releases and
other documents are available on the agency’s Web site, at www.nrc.gov/).
Following the steam-release accident in February 2000, there was a flurry
of letters, press releases and stern warnings from public officials.
U.S. Rep. Sue Kelly (R-Katonah), Westchester County Executive Andy Spano,
Sen. Charles Schumer, Assemblyman Richard Brodsky and others sought
to keep Con Ed from reopening the plant without first replacing the
faulty generators. Accusations of negligence were leveled at Con Ed
and the NRC, and Kelly even wrote then-President Clinton, demanding
that any decision to allow the plant to reopen be made at the highest
levels of the NRC, not by low-level NRC staffers, whose conduct, she
said, “has proven to be questionable.” Even Governor George Pataki weighed
in, signing a law barring Con Ed from recouping the costs of the outage
from customers. The suddenly-fashionable anti-Indian Point bandwagon
gave hope to anti-nuclear activists like Michelle Riddell of New Paltz,
who was arrested with three other people in July after chaining herself
to the doors of Con Ed’s New York office, to protest the planned restart
of IP2 with the faulty generators still in place.
Riddell doesn’t
believe Indian Point is an accident waiting to happen. She says it’s
happening. Referring to the periodic planned releases that are typical
of nuke plants, Riddell says, “It’s like they fart—it’s silent but deadly.
They fart or burp radioactivity.” Riddell believes this is a leading
cause of the high strontium-90 levels in the teeth of Ulster County
babies (see sidebar). Referring to the public relations tactics of nuke
owners, she says, “They don’t mind killing the sheep, they just don’t
want to have us panic. This is their MO” Riddell and others say there’s
no need for Indian Point. They point to New York Assembly hearings of
1994, during which testimony showed that other energy options are cheaper,
that IP3 has run at only 42 percent efficiency over its lifetime, that
it ranks 95th out of 109 US nuclear plants in its lifetime capacity
factor and that rate payers could have saved up to $140 million/year
from closing IP3. When Indian Point was in the news and an election
was on the horizon, activists like Riddell saw at least some of their
views gain widespread political support in NYS. With the new generators
installed and the election over, the ruffled politicians seem to have
been mollified, and the anti-nuke people are on their own once again.
For its part, Con Ed is getting out of the power generation business.
The move is mandated
by the state Public Service Commission pursuant to recent deregulation
of New York State energy producers. What’s Next? Entergy, the company
that will shortly assume ownership of both IP plants, is in the process
of merging with the FPL Group (Florida Power and Light) to create an
industry giant. The combined company will be the nation’s largest electric
utility and power producer, serving more than 6.3 million customers
with a generating capacity of more than 48,000 megawatts, over 10,000
of which will be nuclear-generated. This makes Entergy/FPL the nation’s
second largest nuclear power producer. The merger is slated to be complete
before the end of the year. According to Entergy’s Northeast Communications
Manager, Larry Gottlieb, Entergy rigorously inspects every plant it
buys.
“There’ve been
a lot of operational and management changes [at IP3] that reflect Entergy’s
philosophy of putting safety first,” says Gottlieb. Entergy already
has offices at IP2; as the transfer nears completion, Entergy will be
finalizing a list of plant upgrades and management changes, based on
its own inspection and that of the NRC. “There haven’t been any major
surprises,” Gottlieb says of the NRC report. Most of the work on IP2,
he adds, will probably center around “work systems”—the way in which
problems are analyzed and addressed. This was one of the major issues
for which the NRC faulted Con Ed.
While not speaking
to issues of how Con Ed ran IP2, Gottlieb says Entergy’s strategy is
to empower employees to make decisions. He cites an instance at the
Pilgrim reactor in Plymouth, MA, also recently purchased by Entergy,
where the system was taken off line after an employee heard a suspicious
rattle in the machinery. “Any employee at any time has the right to
go directly to the NRC to voice a concern,” Gottlieb says. “That’s not
frowned upon... that’s our policy.”
“A plant that isn’t
run safely is not economical,” he adds. Gottlieb says his company has
been working closely with officials from Westchester, Rockland, Orange
and Putnam counties on the mandatory 10-mile radius emergency evacuation
plan for Indian Point. The plan will still not be tested every two years
for each plant, he says, because the NRC doesn’t believe more frequent
tests to be necessary.
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